Computer Control ProblemThe computer control malfunction is more unfortunate, and actually has nothing to do with the computer. Originally it was thought the code was somehow malfunctioning, and despite nothing being found it is currently in a state of rework to add additional functionality. This included burn durations that are not integer values (2.5seconds, for example).
I took the opportnity earlier in the week to completely rewire the controller. It was an awful mess of wiring which made it impossible to debug. It also used a lot of high gauge solid conductor wiring, which is rather fragile and easy to break. In fact, the manual ignition firing button was having an intermittent problem likely attributed to a break in the wiring.
So, it was time to gut the controller and rewire it with lower gauge stranded, and minimize all the back-and-forth between the terminal strip and the console buttons by wiring the console buttons up directly to each other. Electrically speaking it would be identical to the old configuration.
Or that was the plan. While everything is working on manual control, the computer control is experiencing some faults. One problem is that when the flow is armed, but ignition is not, the flow is engaged. The second problem is that when the computer is commanding both to engage, as it should be during the ignition/flow startup sequence, neither event is actually on. This results in a very short ignition event, a pause, and then a flow event. This clearly wouldn't result in a good start. The exact circuit error has not been uncovered yet, but will clearly have to be resolved before the next test attempts, currently slated for Wednesday of next week.
Manual controlSo the first three attempts were done with a faulty automatic sequence, and the last four were done under manual control. This was rather reminiscent of the tests last summer, when there was no computer control. As such, attempt 'D' was ignition, and then flow as soon as combustion was seen. Failing that, attempt 'E' was simultaneous flow and ignition. Attempt 'F', done this morning, was preflow, and it literally blew the igniter out of the motor. Attempt 'G' was another preflow attempt, with the igniter held secure with some tape.