Monday, December 24, 2007
Wednesday, December 19, 2007
50N paraffin motor parts machined
We are nearing the end of manufacturing the new parts for the paraffin ~50N motor. We decided not to go for testing on Friday 12/14. A few more parts have yet to be made, such as the mount for the motor, the nozzle insert which will be milled, and the combustion chamber needs the retention holes to be milled. The team also needs to work on the grain manufacturing. We need to do some density testing as well as structural testing. Right now we are also looking for paper tubes with an OD of 2".
Here are some photos of the completed parts.
Here are some photos of the completed parts.
Wednesday, December 12, 2007
Design and Machining in hopes for a test at the end of the week.
So wondering what we are up to?
Well, there have been countless nights with little sleep getting ready for new testing and a nicer motor. At the moment the motor is mostly completed... I will be able to post many more photos and more detailed analysis information. But here are the general concept photos:
Here is the most updated CAD model. 3" OD with 2" ID. Most parts are aluminum where the nozzle inset is Graphite.
Here is the nozzle holder being machined. Not a great photo but I'm usually too busy to take photos. In the photo is a ~3x3x2 in billet being machined by a 3/4 End mill in a HASS VF4. We are only too lucky to have a fantastic machine shop at our disposal. At the moment I had just figured out how to fix a problem having large chord heights on the circular parts. I have never had this problem in the VM3 that I normally use, however I had made some errors in Gibbs CAM. The parts all look much better now.
Well, there have been countless nights with little sleep getting ready for new testing and a nicer motor. At the moment the motor is mostly completed... I will be able to post many more photos and more detailed analysis information. But here are the general concept photos:
Here is the most updated CAD model. 3" OD with 2" ID. Most parts are aluminum where the nozzle inset is Graphite.Saturday, December 8, 2007
Batteries - we eat them like candy!
We did not have a burn on Friday since the new test stand is being rebuilt to provide more reliable load cell readings. The team has been working quite hard on the paraffin design in an effort to get the first paraffin burn before term end.
So, in the meantime, I thought it'd be fun to talk about what electrically powers everything we have. That means batteries. Lots of batteries. So here's the inventory:
Hybrid Launch Controller
So, in the meantime, I thought it'd be fun to talk about what electrically powers everything we have. That means batteries. Lots of batteries. So here's the inventory:
Hybrid Launch Controller
- 2x 9v batteries in series - drives lamps and 5v regulator for control logic output board.
- 1x 9v battery - drives 5v regulator and other circuitry for signal conditioning.
- 1x 28v bench supply - not a battery, but provides the full operating range for the pressure transducers for maximum resolution.
- 2x 9v batteries in parallel - energizes the relays. Recently added trickle-recharge function.
- 1v 12v lead acid - powers nitrous solenoid, pyrogen igniter, dump solenoid (when implemented), and indicator lamps. Also trickle-recharges the 2x 9v batteries when connected.
Thursday, December 6, 2007
Controller / DAQ interface
Above is a partial schematic of the hybrid controller and the relay box. I'd like to discuss some of the gritty technical details behind the black box. It serves as a central interface between human input (arming, manual control), the control computer (timing of ignition & flow), the relay box (and in turn the nitrous solenoid and pyrogen igniter) and finally the data acquisition unit and its computer.
Its this last interface (controller/DAQ) that has been recently added and was giving us trouble on #9 and #10. It is already on its third iteration. The first was a parallel hookup identical to the lines going to the relay box. This proved problematic since this interface betweens float (logic low) and ground (logic high). While it may be possible for the DAQ to sense this, it isn't ideal since it adds the potential for a malfunction in the DAQ or the associated wiring to trigger an event.
The second iteration provides that needed layer of isolation through the use of a quad NAND gate (CD4011). It also provides readable voltages that is easier for the DAQ to handle. This is the 5v logic low and 0v logic high mentioned in the previous post. The oscillations shown in that graph are because the operating voltage of the NAND gate (5v) is lower than the operating voltage of the relay box (9v). The NAND operating voltage has to be higher, so the easy thing is to up the voltage to 12v or even the 18v that the controller's lamps run on.
Of course, the solution creates a new problem. The DAQ can only accept 0-5v, so the output of the NAND gate has to be bumped down somehow. The solution is a op amp configured as a comparator (LM339). Combined with a resistor bridge (voltage divider) across the NAND's power source, the op amp will check whether the op amp's input is higher or lower than the divider's halfway point. Its output will thus be either 0v or 5v accordingly.
Phew! And that's what is necessary to safely get the controller's logic into the DAQ.
Wednesday, December 5, 2007
Good burns, but w/out data did it really happen?
Tuesday had two successful burns that premiered a few upgrades. They are:
Why we have all the ignition trouble is still a bit of a mystery. Best guess is that the pyrogen on the igniters degrade over time, and these are approaching a year old since they were built for WARRIORS II. A new batch is needed, and perhaps this will get us to the point where we don't need the augmentation anymore (which was the case for tests #2-#6).
This is the burn from #10. The white line is the chamber pressure, green is supply pressure. It seems the configuration of the cart is such that it doesn't move freely ("frictionless") so we didn't get good load cell data. The test stand has to be redesigned & rebuilt; this should be ready to debut for #11. More details to follow of course.
The blue line is the flow logic line from the controller. Yes, it was a bit upset w/ me at the time of the tests, and would oscillate between 0v and 5v when logic low, but would stay at 0v when logic high. Yes, that may seem a little backwards to you - 0v for on, 5v for off. I selected this so that you know that the logic line is working before you start the burn. Otherwise what would 0v mean? That the valve was off or that the logic line was disconnected or otherwise fouled?
At any rate, the problem was solved, but it resulted in the output voltage exceeding the 5v that the DAQ can support. So more electronics get crammed into the controller to ramp it back down. It will be ready to support #11 and #12, which are planned for this Friday. The ignition logic will also be included.
Sadly, due to a foulup w/ LabView, that pretty picture above is all the data we have. While we were able to see everything in real time, none of it was saved to the hard disk. We were lucky to still have the window open to take a screenshot of the graph from #10. Nothing survived from #9 at all, although visually the burns were very similar.
10s burns seems to be at the limit of what the 5lbf PVC configuration can handle. The cutaways of the grains (we used a fresh grain for #10) revealed the core diameter nearly matches the diameter of the injector & nozzle.
- Chamber Pressure Transducer (~62psi)
- Long burn (10s apiece)
- Metal braided nitrous oxide delivery line
- Controller state output to DAQ (partial)
- Improved computer control code (advanced settings menu)
Why we have all the ignition trouble is still a bit of a mystery. Best guess is that the pyrogen on the igniters degrade over time, and these are approaching a year old since they were built for WARRIORS II. A new batch is needed, and perhaps this will get us to the point where we don't need the augmentation anymore (which was the case for tests #2-#6).
This is the burn from #10. The white line is the chamber pressure, green is supply pressure. It seems the configuration of the cart is such that it doesn't move freely ("frictionless") so we didn't get good load cell data. The test stand has to be redesigned & rebuilt; this should be ready to debut for #11. More details to follow of course.The blue line is the flow logic line from the controller. Yes, it was a bit upset w/ me at the time of the tests, and would oscillate between 0v and 5v when logic low, but would stay at 0v when logic high. Yes, that may seem a little backwards to you - 0v for on, 5v for off. I selected this so that you know that the logic line is working before you start the burn. Otherwise what would 0v mean? That the valve was off or that the logic line was disconnected or otherwise fouled?
At any rate, the problem was solved, but it resulted in the output voltage exceeding the 5v that the DAQ can support. So more electronics get crammed into the controller to ramp it back down. It will be ready to support #11 and #12, which are planned for this Friday. The ignition logic will also be included.
Sadly, due to a foulup w/ LabView, that pretty picture above is all the data we have. While we were able to see everything in real time, none of it was saved to the hard disk. We were lucky to still have the window open to take a screenshot of the graph from #10. Nothing survived from #9 at all, although visually the burns were very similar.
10s burns seems to be at the limit of what the 5lbf PVC configuration can handle. The cutaways of the grains (we used a fresh grain for #10) revealed the core diameter nearly matches the diameter of the injector & nozzle.
Monday, December 3, 2007
Recalibrating and DAQ setup
Well work has been continuing since the last test, we have been working on setting up the DAQ so that the control interface is also recorded, such that we will have the time and duration for each event. This way we will know exactly when the solenoid is open and when ignition happens as well as when the solenoid is closed.
The pressure transducers have each been calibrated twice. We noticed that even though during the first round of calibration, the excitation voltage dropped from 28-23 V, we recorded ~ P psi=194.4x-27.34 where X is the voltage output. We recalibrate from a power supply, which will give us a much safer constant voltage. With this setup the transducers were P(psi)=204.1x-4.5 (between the two transducers, the y intercepts are a bit different). This however is fine, and we now have a reliable method of obtaining delivery pressure. Just to mention, we used a helium tank with a regulator and a well calibrated pressure dial indicator for pressure calibration. Not the best possible method, but this will do us well.
The pressure port was drilled today and looks great, we should have minimum pressure loss, though there is some worry that with all the extra volume that we have added that must be pressurized, there must be some way to fill this volume with some non combustible material. One though is krytox, however that would be Very expensive as it would require alot to fill the 90 elbow and lines for the transducer.
Other members machined another fuel grain and we should see two 10 second tests tomorrow around noon!
The pressure transducers have each been calibrated twice. We noticed that even though during the first round of calibration, the excitation voltage dropped from 28-23 V, we recorded ~ P psi=194.4x-27.34 where X is the voltage output. We recalibrate from a power supply, which will give us a much safer constant voltage. With this setup the transducers were P(psi)=204.1x-4.5 (between the two transducers, the y intercepts are a bit different). This however is fine, and we now have a reliable method of obtaining delivery pressure. Just to mention, we used a helium tank with a regulator and a well calibrated pressure dial indicator for pressure calibration. Not the best possible method, but this will do us well.
The pressure port was drilled today and looks great, we should have minimum pressure loss, though there is some worry that with all the extra volume that we have added that must be pressurized, there must be some way to fill this volume with some non combustible material. One though is krytox, however that would be Very expensive as it would require alot to fill the 90 elbow and lines for the transducer.
Other members machined another fuel grain and we should see two 10 second tests tomorrow around noon!
Thursday, November 29, 2007
Wednesday, November 28, 2007
Testing and Data = engineers party
First test went off without a hitch.
Here are pics... they do better than words
I'll upload photos of the Data and a detailed description of what is going on.
Thrust Curves


Monday, November 26, 2007
Blog is up, where we are
Well its up and running. We will now be posting daily updates or maybe weekly depending on how easy this seems.

So far we have setup all the hardware and are preparing for the 2nd testing attempt. This should take place on 11/28. This will be the test of two 5 lb motor firings using the PVC grain developed by the summer crew.
Next will be a test of a 25lb PVC motor. And after that, the paraffin fun will begin! Here is the new motor set up without the mounting plates or motor mount
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